PRESS RELEASE
11 April 2003, Wichita Falls, Texas
It has been several
months since the last press release and the last time the CarterCopter
Technology Demonstrator (CCTD) was flying. We have been busy working on
several major changes and improvements to the aircraft, most notably a
new high-m
rotor, and boosted, automated controls.
Flight Tests Superb - Unfortunate
Ending

Flight-testing
of the CCTD began again on March 30th, 2003. After a few days of
high-speed taxi runs, making minor adjustments, and debugging, the aircraft
was flown in the traffic pattern. The new rotor worked well in the
flight regimes tested. The dual redundant boosted controls worked
perfectly (better than expected) in most areas, plus the control forces
were still manageable when the boost system was disengaged. The
automated controls are much improved, although some software tweaking
is still needed. During one 19-minute flight, the automated controls
were engaged for about 18 minutes and in most cases could hold the rotor
rpm and flapping more accurately than the pilots. These controls
reduce the pilot workload, and once perfected, will make the aircraft
so easy to fly that grandmother and granddaddy might want to take up flying.
By the end of flight-testing on April 7th we had a total of
2.9 hours of accumulated flight time showing marked improvement with the
new systems. Our longest flight was 37 minutes and our top speed
was 132 mph.
On April 8,
2003, the flight began with a short takeoff using about 20 ft of runway.
The gear was retracted, and several high-speed passes were performed.
The day's flight regimen was intended to test the complete range of the
CCTD's flight controls and it performed superbly. At the end of
its flight, the aircraft entered final at about 1500 ft, and began a nearly
vertical descent to the runway. The descent was at about 1000 fpm,
and was so quiet that the aircraft could barely be heard from the ground.
Unfortunately, the pilots failed to lower the landing gear (however
it was not just the pilots' fault). This was only their second gear retraction
in the past 7 months as most of the test flights had been made with the
gear extended. They did not realize their error until about 30 ft AGL
(heard it on the radio). The pilot in command made the decision
to attempt a go-around. He gave the aircraft full throttle
and pulled back on the stick to try to climb. Sadly, they were too
low and ended up flying the aircraft into the runway at full throttle/rpm.
The impact was enough to deflect the tailbooms sufficiently for the propeller
to strike the ground. When this happened, one propeller blade broke
away, leaving the driveshaft unbalanced for nearly one revolution until
the second blade came off, damaging many components in the engine compartment,
including the engine. The aircraft slid on the fuselage and tailbooms
for approximately two hundred feet before coming to a stop. The bottom
of the wing/fuselage was ground off to the fuel tank. Had we not
located a separate fuel tank for testing in the very strong pressurized
cabin, we could have had a major fire. Repairs will add a Kevlar
abrasion pad in this area for enhanced future safety. This gear-up landing
also resulted in substantial damage to the engine compartment, fuselage
and tailbooms. However, it is very important to note that the pilots never
felt in danger and walked away from the aircraft with no injuries.


After examining
the aircraft, we believe that it can be rebuilt and flying again within
3½ months. This downtime provides an opportunity to make several
improvements that might not have been performed until much later.
The engine will be replaced with a new, turbocharged engine. Without
the turbo installed, this engine should produce 425 HP at sea level, or
100 HP more than the current engine. But with the turbo installed,
the engine will be able to maintain that horsepower up to 25,000 feet.
The power train that was designed for the Next Generation CarterCopter
(NxCC) has the capacity for 700 HP and will replace the one that was damaged
in the accident. A new scimitar propeller will be designed and built.
This propeller will sacrifice approximately 1% cruise efficiency for a
5 -10% increase in takeoff and climb performance.
Several military VIPs
were visiting to observe the flight-testing and discuss possible funding
for the Next Generation CarterCopter (NxCC). They were very impressed
with the performance of the CCTD, and did not appear to be discouraged
by the accident. In fact, after the flight, one of them stated that
it was one of the most impressive flight demos that he had ever seen,
and that he now better understood the significance of this technology.
A more detailed press release is currently
being prepared. It outlines the efforts of the last 4 months and some
of our future prospects. It will also include more details about
the latest round of flight-testing, more info about the accident and changes
we plan to make while repairs are being made.
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